缩放比例
井筒
石油工程
天然气田
环境科学
材料科学
气体成分
化学
生产(经济)
放气
扫描电子显微镜
矿物学
领域(数学)
致密气
衍射
比例(比率)
机制(生物学)
化学成分
作者
Xiaofeng Dang,Yang Liu,Liping Liu,Chen Hu,Yuntao Xi
出处
期刊:Journal of physics
[IOP Publishing]
日期:2025-09-01
卷期号:3048 (1): 012177-012177
标识
DOI:10.1088/1742-6596/3048/1/012177
摘要
Abstract The scaling in tubing is a serious problem in Jingbian gas field, which leads to the increase of low production and low efficiency wells year by year. The production capacity of gas wells cannot be utilized effectively. In this paper, the scanning electron microscopy (SEM) was used to characterize the morphology of scale, and energy dispersion spectroscopy (EDS) and X-ray diffraction (XRD) were utilized to analyze the composition of scaling products. According to the design of the plugging removal scheme, the scale-dissolving test of acid plugging remover was carried out. The results show that the scale samples have a three-layer structure, and the morphology of the three layers is quite different, but the chemical composition of the three layers is CaCO3. After adding acid plugging removal agent, the scale-like reaction is severe, a lot of gas escape, 40 h completely dissolved, no solid residue. Based on the test results and the production situation of Jingbian gas field, the scaling mechanism of gas wells is clarified, and the plugging removal scheme is optimized, which provides a basis for increasing production and efficiency of Jingbian gas field.
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