冲孔
升级
自动化
西门子
过程(计算)
控制系统
计算机科学
工程类
汽车工程
模拟
机械工程
电气工程
操作系统
作者
Dangfeng Pang,Shigang Cui,Yongli Zhang
标识
DOI:10.1109/itoec53115.2022.9734694
摘要
In order to improve the working efficiency and safety of the stainless steel spoon punching, after analyzing the punching and cutting process and the production requirements of enterprise, a precision positioning control system for the automatic feeding device based on integral separation PID algorithm is designed. The system uses Siemens S7-200SMART PLC as the master station. Design parameters and display data through the touch screen, and use DC motors and pneumatic circuits to achieve coordinated control of the punch and feeder. Through actual production verification, the system has high relocation accuracy and reliable operation, the efficiency increased by 40%. At the same time, it reduces safety hazards and labor costs, provides a reference and theoretical basis for the automation upgrade and transformation of stamping feeding.
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